Fan Drive pillow block shaft
 

Fan Drive pillow block shaft

Started by Emcemv, August 16, 2014, 06:12:23 PM

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Emcemv

Some of you may remember my post a few months back about how my fan drive shaft had been spinning in the bearing and the race had worn a 1/8" deep groove in the shaft.  My MC-7 is a combo and has the scenic side radiator so has the fan driven through a right angle drive and the shaft sits in a pillow block with 2 big ball bearings.  Since the shaft was pretty much not available anywhere, I had the old shaft welded up and re-turned to make it new again.  At the time many of you cautioned that the welding would warp the shaft and it did but the machining was able to take care of it, it only warped about .003".  So I got it back yesterday and it looks beautiful and I got it back together today....$45.00 for the welding and a freebie from a machinist friend.  Here's some photos
Bruce & Nancy Fagley
1973 MCI MC-7 Combo Freighter
450HP DD 8V-92T 2000 Reman
HT 740 Allison
Woodbury CT.

wildbob24

P8M4905A-1308, 8V71 w/V730
Custom Coach Conversion
PD4106-2546, 8V71, 4sp
Greenville, GA

luvrbus

Very nice job that is the way I am doing the obsolete S cams on some Eagles
Life is short drink the good wine first

eagle19952

you found an excellent welder, had you not we'd be looking at a paper weight.
happy you took the leap..... ;D
Donald PH
1978 Model 05 Eagle w/Torsilastic Suspension,8V71 N, DD, Allison on 24.5's 12kw Kubota.

Emcemv

To Weld it, he chucked it in a lathe and turned it at real slow speed and welded as it rotated, I think that kept the heat pretty even and cut down on the warping.  Bearings were a slight press fit and we used red locktite on them as well.  I think this all started because there was a spacer missing, there was nothing to hold the shaft in place on its length so once it started to move, it just got worse and worse.  Now I have a spacer made to locate the pulley and prevent the shaft from moving in and out.
Bruce & Nancy Fagley
1973 MCI MC-7 Combo Freighter
450HP DD 8V-92T 2000 Reman
HT 740 Allison
Woodbury CT.

eagle19952

Quote from: Emcemv on August 16, 2014, 07:47:43 PM
  I think this all started because there was a spacer missing, there was nothing to hold the shaft in place on its length so once it started to move, it just got worse and worse.  Now I have a spacer made to locate the pulley and prevent the shaft from moving in and out.

sounds like you solved it....often no one asks/solves why long enough to fix the cause.
Donald PH
1978 Model 05 Eagle w/Torsilastic Suspension,8V71 N, DD, Allison on 24.5's 12kw Kubota.

luvrbus

The guy that does my S Cams uses a Arc spray process it works good
Life is short drink the good wine first

brmax

That's a great job and better yet to have the good friends.
Is that Spray process actually have a powder type metal they use with welding
1992 MC9
6V92
Allison

Lee Bradley

A little late now but if you go to a crankshaft shop they are set up for welding and turning shafts to thousandths of an inch.

luvrbus

A automotive machine shop does my S cams the same process they use on cranks
Life is short drink the good wine first